Register Community Calendar Today's Posts Search

Go Back   GZ 250 Forums > GZ250-Specific > Troubleshooting

Reply
 
Thread Tools Display Modes
Old 07-28-2017, 07:01 AM   #1
new_bee
Junior Member
 
Join Date: Jul 2017
Posts: 8
Lacking power in 3/4/5 gear

New gz250 owner (2003 15k miles).. seemed to run great on a brief, back-road test drive.. Luckily it was cheap, and factored in some $ on maintenance, etc..

Honestly the bike seems to run great... it revs up well in neutral.

In first gear the bike accelerates well and buzzes right upto ~25mph, and upto 35mph+ in 2nd gear... in 3rd/4th/5th, I can get the bike upto ~45 (barely maybe 50mph downhill)... in 4th and 5th the bike just won't speed up much at all.

There are a few similar helpful posts..but nothing conclusive!

I have gone through and read a lot, downloaded the service & owners manuals, and done searches on this forum & google, and I think I have covered most of the basics..

A couple quick notes:
-previous owner had the oil about 1/4-1/2 quart overfilled. not sure type of oil or anything, or for how long, but oil didn't look bad when drained.
-in neutral I can hear a slight ticking sound that is not there when in gear, seems like it's possibly from the clutch/ transmission area... not bad or obvious (not sure if this is normal) but noticeable
-old spark plug maybe seemed a little whitish or dry..

So far I have
-Emptied fuel tank, new fuel filter, checked petcock for good flow
-Fresh gas with strong dose of seafoam.
-Drained carb and filled with straight seafoam, then let sit overnight. The gas that drained out of the carb didn't seem visually bad, gelled or anything at all..
-Fresh motorcycle rated oil
-New air filter
-New plug
-Adjusted clutch cable, set to dime gap, then tried going for extra slack/play before it engages to be sure.
-Bike coasts well so it doesn't seem like any extra resistance anywhere.
-Tested for air leaks around intake boots and rubber hoses by spraying starter fluid around those areas while running, no change in idle speed. Tank vent is working.


I haven't yet pulled the carb for a clean/rebuild, or checked the valve clearances, or checked the compression yet.

I have put about 50 miles on it after doing the things listed above and it hasn't changed much at all..so I don't think it really feels like a carb issue that is going to clear up with carb cleaner in the gas.


I am hoping, at this point that a full carb cleaning will be all it needs! Really crossing my fingers because beyond that, I might be hiring a mechanic.

If that doesn't do it, next I will try to figure out if adjusting/checking the valve clearances is something I can do myself.

Finally, I wonder if anyone can describe or link me to any references for checking or evaluating if this might be an issue caused by the clutch? (clutch slippage)

IS THERE ANYTHING I AM MISSING?

thoughts, advice or encouragement greatly appreciated! thanks!



Login or Register to Remove Ads

Last edited by new_bee; 07-28-2017 at 07:05 AM.
new_bee is offline  
Reply With Quote
Old 07-28-2017, 11:38 AM   #2
Fawlty
Senior Member
 
Fawlty's Avatar
 
Join Date: Jan 2013
Location: Murcia, Spain
Posts: 683
If the bike has a 16 tooth rear sprocket, you can expect some loss of power in 4th and 5th. Worth checking.
__________________
"It begins here for me on this road. How the whole mess happened I don't know, but I know it couldn't happen again in a million years."

(Johnny Strabbler-The Wild One 1953)
Fawlty is offline  
Reply With Quote
Old 07-28-2017, 02:20 PM   #3
Vegas Street Rider
Senior Member
 
Join Date: May 2015
Location: Henderson, NV
Posts: 1,108
I have a 16 tooth front sprocket and although it is not as peppy in 4th and 5th, I still have plenty of power to take it up to 70/75 mph on the flat with no head wind. I don't think that is a factor.



Login or Register to Remove Ads
Vegas Street Rider is offline  
Reply With Quote
Old 07-29-2017, 01:03 AM   #4
new_bee
Junior Member
 
Join Date: Jul 2017
Posts: 8
Stock sprockets/gearing g.

Anything else I should check before I pull the carb as the next step?
new_bee is offline  
Reply With Quote
Old 07-29-2017, 08:26 PM   #5
new_bee
Junior Member
 
Join Date: Jul 2017
Posts: 8
Carb rebuild did it. I think the carb was perfectly clean, but possibly the diaphragm was pinched on the upper portion around the lip where it seals.



Login or Register to Remove Ads
new_bee is offline  
Reply With Quote
Old 07-31-2017, 12:50 AM   #6
5th_bike
Senior Member
 
5th_bike's Avatar
 
Join Date: Oct 2007
Location: HoCo, Maryland
Posts: 1,349
Good. To finish things off, I'd check the valve clearances.
__________________
2005 "Saturn Black", stock + tach
5th_bike is offline  
Reply With Quote
Old 08-22-2017, 11:02 PM   #7
new_bee
Junior Member
 
Join Date: Jul 2017
Posts: 8
So after around 20 miles of running, the problem was back. It seems like the same exact symptoms, lacking power, and the symptoms seems to have come on fairly quickly.

I believe the diaphragm might not be sealing correctly in the grove, I took it apart twice, the second time I put it back together with a small amount yamabond adhesive around the o ring, but still runs the same. I've ordered a new diaphragm but not sure if I should have ordered the whole diaphragm slide assembly.

I checked the valve clearances and they are within special. But I noticed a minor oil leak behind the left top engine access cover.
I wasn't really able to identify where it was coming from.

Any thoughts on either issue appreciated
new_bee is offline  
Reply With Quote
Old 08-23-2017, 02:25 PM   #8
Vegas Street Rider
Senior Member
 
Join Date: May 2015
Location: Henderson, NV
Posts: 1,108
Check the head bolts. Left top oil leak seems to be pretty common with the GZ. I had a minor leak and after torquing the head bolts, all is well.
Vegas Street Rider is offline  
Reply With Quote
Old 08-24-2017, 01:01 PM   #9
derbydave
Senior Member
 
derbydave's Avatar
 
Join Date: Jan 2017
Location: KS
Posts: 103
Is there junk in the tank that is clogging a jet? I would clean the carb again and install an inline filter in the fuel line. A problem with the diaphragm sounds unlikely. It doesn't take very much at all to plug up a jet
__________________
2003 Suzuki GZ250 (Sold)
1986 Suzuki Cavalcade LXE
1986 Suzuki Intruder VS700
derbydave is offline  
Reply With Quote
Old 08-25-2017, 01:15 AM   #10
new_bee
Junior Member
 
Join Date: Jul 2017
Posts: 8
There's a new inline filter (old wasn't bad), and tank is clean.. No junk in carb at all both times I cleaned it.

Thanks for heads up on head bolts
new_bee is offline  
Reply With Quote
Reply




Posting Rules
You may not post new threads
You may not post replies
You may not post attachments
You may not edit your posts

BB code is On
Smilies are On
[IMG] code is On
HTML code is Off

Forum Jump


All times are GMT -4. The time now is 10:52 PM.


Powered by vBulletin® Version 3.8.4
Copyright ©2000 - 2024, Jelsoft Enterprises Ltd.